Can you post a schematic of what you eventually went with?
Thanks - and congratulations on getting it working!
Hi ledtester,
Boring old germanium diode bridge wired across the motor terminals, 10K pot from +output of that to gnd, with very tiny greencap (3mm x 8mm x 2mm) and 4V7 clamp zener from wiper output to gnd.
The running motor is disabled for 2ms, each 1/12th of a second, after which period the back EMF from 2 successive measurements is averaged.
Yet to be properly tuned PID does the rest. A small Kp, much larger Ki, and almost none, but some very small Kd.
Sorry, a diagram would be just scribble, as I'm still recovering from an 'accident' with the hard drive I kept all those type of programs on. I hope the description was clear enough for anyone to follow.
Thanks very much for your interest, and fabo suggestions, everyone.

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